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射阳闸闸下感潮河段电厂码头和取水工程淤积研究
引用本文:徐群,陆瑞兴,马启南,王俊,蒋燕.射阳闸闸下感潮河段电厂码头和取水工程淤积研究[J].海洋工程,2006,24(3):49-55.
作者姓名:徐群  陆瑞兴  马启南  王俊  蒋燕
作者单位:河海大学,水资源环境学院,江苏,南京,210098;南京水利科学研究院,江苏,南京,210024;中交第四航务工程勘察设计院,广东,广州,510230;南京水利科学研究院,江苏,南京,210024;河海大学,水资源环境学院,江苏,南京,210098
摘    要:以射阳港电厂三期扩建码头和取水口工程为例,建立射阳闸至河口段物理模型进行水流泥沙试验。试验研究表明,丁坝群并辅以开挖槽方案实施后,电厂河段减淤效果较好,三期取水口前沿河床平均高程从-4.41 m降低到-4.76 m,煤码头前沿港池的平均高程从-3.77 m降低到-4.49 m左右,能满足设计部门的要求。

关 键 词:射阳河  码头  取水口  模型试验  淤积
文章编号:1005-9865(2006)03-0049-07
收稿时间:2005-08-22
修稿时间:2005年8月22日

Research on sedimentation in the tidal reach downstream of Sheyang tide lock
XU Qun,LU Rui-xing,MA Qi-nan,WANG Jun,JIANG Yan.Research on sedimentation in the tidal reach downstream of Sheyang tide lock[J].Ocean Engineering,2006,24(3):49-55.
Authors:XU Qun  LU Rui-xing  MA Qi-nan  WANG Jun  JIANG Yan
Institution:1. College of Water Resources and Environmental Engineering, Hohai University, Nanjiang 210098, China; 2. Nanjiang Hydraulic Research Institute, Nanjing 210024, China; 3. China Communication Fourth Design Institute of Navigation Engineering, Guanzhou 510230, China
Abstract:Taking the wharf and water intake project of the third-phase expansion project of Sheyang Power Plant as an example,the authors construct a physical model from Sheyang tide lock to the estuary to do the experiment on current and sediments.The research shows that it has a good effect on the reduction of sedimentation after the regulation project,that the river bed average elevation at the third-phase water intake declines from-4.41 m to-4.76 m,and that the wharf basin average elevation declines from-3.77 m to-4.49 m.All these can meet the needs of the design department.
Keywords:Sheyang River  wharf  water intake project  experiment  sedimentation
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