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大埋深高地应力关山隧道围岩变形破坏分析
引用本文:梁 宁,伍法权,王云峰,包 含.大埋深高地应力关山隧道围岩变形破坏分析[J].岩土力学,2016,37(Z2):329-336.
作者姓名:梁 宁  伍法权  王云峰  包 含
作者单位:1. 中国科学院大学,北京 100049;2. 中国科学院地质与地球物理研究所 中国科学院页岩气与地质工程重点实验室,北京 100029; 3. 绍兴文理学院 土木工程学院,浙江 绍兴 312000;4. 天平铁路有限公司,甘肃 天水 741020
基金项目:国家自然科学基金(No. 41030749)
摘    要:甘肃省关山隧道是一条受高地应力影响的大埋深硬脆性闪长岩铁路隧道,位于青藏高原东北缘,构造活跃,运动速率较大,且方向变化显著的六盘山挤压隆升构造区。在隧道开挖过程中围岩变形破坏现象明显,围岩等级低于前期岩体质量分级,表现出强烈的岩体质量劣化和各向异性。针对该问题,除了采用矿物成分和微结构分析寻找原因,还通过现场结构面统计分析对围岩质量劣化和各向异性进行描述,同时运用自行研发的钻孔电视进一步分析开挖前后一定时间间隔内围岩的渐进式变形和破坏。钻孔电视试验结果表明,尽管闪长岩作为一种硬脆性岩体,单轴抗压强度(UCS)高于现场地应力值,但其变形和破坏却普遍发生,开挖过程中新生裂隙迅速发育,原先在高地应力下闭合的裂隙也会重新张开和发展,围岩劣化,稳定性降低。为了进一步分析围岩的变形破坏过程,设计了变压力大小和方向的单轴抗压试验,试验中闪长岩的单轴压力值低于单轴抗压强度,试验结果与钻孔电视试验观测结果吻合,证明了在开挖引起的地应力剧烈变化条件下硬脆性闪长岩结构劣化,存在变形破坏的可能性。在大埋深高地应力条件下,除了岩体的各向异性,地应力的变化也是硬脆性围岩稳定性的重要考量因素。

关 键 词:深部硬脆岩体  变形破坏  高地应力  闪长岩  
收稿时间:2016-06-09

Analysis of deformation and failure of rock mass of deep Guanshan tunnel under high in situ stress
LIANG Ning,WU Fa-quan,WANG Yun-feng,BAO Han.Analysis of deformation and failure of rock mass of deep Guanshan tunnel under high in situ stress[J].Rock and Soil Mechanics,2016,37(Z2):329-336.
Authors:LIANG Ning  WU Fa-quan  WANG Yun-feng  BAO Han
Institution:1.University of Chinese Academy of Sciences, Beijing 100049, China; 2. Key Laboratory of Shale Gas and Geoengineering, Institute of Geology and Geophysics, Chinese Academy of Sciences, Beijing 100029, China; 3. College of Civil Engineering,Shaoxing University, Shaoxing, Zhejiang 312000, China; 4. Tianping Railway Corporation Limited, Tianshui, Gansu 741020, China
Abstract:Guanshan railway tunnel, located in Gansu Province, China, is a deep tunnel in hard and brittle diorite rock mass under high in situ stress. Meanwhile, this tunnel is also located in the Liupan Mountain, which is an active tectonic region of the compression uplift with a high horizontal movement rate and significantly changes of movement direction on the northeastern margin of Qinghai-Tibet block. On the contrary of the good rock mass classification predicted in investigation stage, the real situation after excavation shows a great change of rock mass parameters and structure, revealing not only the degradation of rock mass quality also the significant anisotropy of rock mass. The degradation and anisotropy of rock mass is described and analyzed based on the statistic analysis of the rock structural plane in field. Meanwhile, self-developed borehole camera is adopted to further observe the progressive deformation and failure of rock mass in an interval after excavation. As one of the hard and brittle plutonite, the uniaxial compressive strength (UCS) of diorite is a relatively high index on investigation stage, which is obviously larger than the in situ stress. However, the deformation and failure of diorite rock mass happened prevailingly. As the evidence obtained by borehole camera, the micro fracture or closed rock structural plane under high in situ stress will re-open and develop quickly after the excavation, which degraded the stability and quality of rock mass structure. To figure out the deformation and failure process, an angle rotation of uniaxial compressive test is designed. The uniaxial pressure is lower than the uniaxial compressive strength of diorite. This test has good agreement with the borehole camera test results, fully presents degradation of rock mass structure, induced by stress field change after excavation and proves the feasibility of the progressive deformation and failure process of hard and brittle diorite rock mass during the strongly stress field change after excavation. Besides anisotropy of rock mass, stress field change is always a significant consideration factor in deep excavation project under high in situ stress.
Keywords:deep hard and brittle rock mass  deformation and failure  high in-situ stress  diorite  
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