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南阳凹陷致密储层钻井液损害评价及酸化改造对策研究
引用本文:向阳,向丹.南阳凹陷致密储层钻井液损害评价及酸化改造对策研究[J].矿物岩石,2001,21(4):71-74.
作者姓名:向阳  向丹
作者单位:成都理工大学
摘    要:本文通过矿物使用的钻井液和酸化解堵液对储层岩石所作的损害评价试验证实,该区储层产能低的原因之一是钻井液和酸化解堵液使储层渗透率损害达35%-75%造成。针对该区储层实际,采用作者研制的酸液解堵模拟试验证实,可使储层渗透率恢复到原始值的89%-185%,平均恢复至原始值的110%,适用于该区储层的酸化解堵。

关 键 词:地层损害  钻井液  酸化液  GFP-200酸液  致密储层
文章编号:1001-6872(2001)04-0071-04
修稿时间:2001年9月11日

EVALUATION OF THE DAMAGE OF DRILLING FLUID TO THE TIGHT RESERVOIR IN NANYANG SAG AND RESEARCH ON ACIDIZATION ALTERATION COUNTERMEASUE
XIANG Yang XIANG Dan State Key Laboratory of Oil and Gas Reservoir Geology and Exploitation,Chengdu University of Technology,Chengdu.EVALUATION OF THE DAMAGE OF DRILLING FLUID TO THE TIGHT RESERVOIR IN NANYANG SAG AND RESEARCH ON ACIDIZATION ALTERATION COUNTERMEASUE[J].Journal of Mineralogy and Petrology,2001,21(4):71-74.
Authors:XIANG Yang XIANG Dan State Key Laboratory of Oil and Gas Reservoir Geology and Exploitation  Chengdu University of Technology  Chengdu
Institution:XIANG Yang XIANG Dan State Key Laboratory of Oil and Gas Reservoir Geology and Exploitation,Chengdu University of Technology,Chengdu 610059
Abstract:Trough the experiment of damage to reservoir rock,caused by drilling and acidizing fluid, this paper revealed that one of the causes of low productivity in the Nanyang sag is the damage of drilling and acidizing fluid to reservoir permeability,which reached 35%~75%.In order to solve the problem,we made simulation test by using acidizing fluid developed by us to eliminate the blokage in the reservior.The test achieved effective result,characterized by recovery of reservior permeability to 89%~185%,with an average value of 110%.The acidizing fluid proved to be suitable for the blokage elimination in the reservior of the Nanyang sag.
Keywords:formation damage  drilling fluid  acidizing fluid  GFP-200 acidizing fluid
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