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充气钻井技术在油砂山油田的应用实践
引用本文:郑锋,李霖,郗凤亮,柳鹤,王磊,房旭,关敬.充气钻井技术在油砂山油田的应用实践[J].探矿工程,2018,45(2):18-21.
作者姓名:郑锋  李霖  郗凤亮  柳鹤  王磊  房旭  关敬
作者单位:渤海钻探工程技术研究院,渤海钻探第一钻井分公司,渤海钻探钻井技术服务分公司,渤海钻探工程技术研究院,中国石油集团钻井工程技术研究院,渤海钻探第一钻井分公司,渤海钻探工程技术研究院
基金项目:中石油渤海钻探工程公司重大科研项目“青海油田油砂山优快钻完井技术研究”(编号:2017ZD16Y)
摘    要:柴达木盆地油砂山油田地质构造复杂,地层孔缝发育、压力系数低,常规泥浆钻井过程中漏失频繁、钻井周期长,严重制约了勘探开发效益。针对该地区钻井难点,进行了4口井充气钻井试验。试验结果表明,充气钻井能有效解决油砂山油田漏失地层钻井问题,并提高机械钻速,与常规泥浆钻井技术相比,平均节约堵漏时间6.32 d,漏失量减少54.5%,机械钻速提高1.1倍。试验的成功,对该区块优快钻井技术的研究和推广应用具有指导意义。

关 键 词:充气钻井  井漏  堵漏  机械钻速  油砂山油田
收稿时间:2017/7/29 0:00:00
修稿时间:2017/10/11 0:00:00

Application Practice of Aerated Drilling Technology in Youshashan Oilfield
ZHENG Feng,LI Lin,XI Feng-liang,LIU He,WANG Lei,FANG Xu and GUAN Jing.Application Practice of Aerated Drilling Technology in Youshashan Oilfield[J].Exploration Engineering(Drilling & Tunneling),2018,45(2):18-21.
Authors:ZHENG Feng  LI Lin  XI Feng-liang  LIU He  WANG Lei  FANG Xu and GUAN Jing
Institution:Engineering Technology Research Institute, Bohai Drilling Engineering Co., Ltd.,No.1 Drilling Company, Bohai Drilling Engineering Co., Ltd.,Drilling Technology Services Company, Bohai Drilling Engineering Company Limited,Engineering Technology Research Institute, Bohai Drilling Engineering Co., Ltd.,Drilling Engineering and Technology Research Institute,CNPC,No.1 Drilling Company, Bohai Drilling Engineering Co., Ltd.,Engineering Technology Research Institute, Bohai Drilling Engineering Co., Ltd.
Abstract:Youshashan oilfield is located at Qaidam basin, the complex geological structure, formation cracks development, low pressure coefficients, frequent leakage and long drilling cycle have seriously restricted the exploration and development benefits in conventional mud drilling. In view of these difficulties, aerated drilling tests are carried out in 4 wells, the results show that the aerated drilling can effectively solve the drilling problems in the leakage formation of Youshashan oilfield and improve the POP; compared with conventional mud drilling technology, the average plugging time is reduced by 6.32 days, the leakage loss is reduced by 54.5% and the ROP is increased by 1.1 times. The success of the tests are of guiding significance for the research and application in optimized and fast drilling technology in this block.
Keywords:aerated drilling  well leakage  plugging  ROP  Youshashan oilfield
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